河北水利电力学院学报 ›› 2018, Vol. 28 ›› Issue (4): 41-43.DOI: 10.16046/j.cnki.issn2096-5680.2018.04.009

• 技术理论与应用 • 上一篇    下一篇

一起箱式变电站屋顶密封不严导致跳闸原因分析及预控措施

叶方舟1,郭书俊2,崔淑娟1   

  1. 1.国网河北省电力有限公司沧县供电分公司,沧州市黄河东路32号 061000;
    2.河北水利电力学院,沧州市重庆路1号 061001

  • 收稿日期:2018-06-04 修回日期:2018-10-12 出版日期:2018-12-31 发布日期:2019-01-31
  • 作者简介:叶方舟(1988-),男,河北沧州人,工程师,现从事的变电运检工作方向等。E-mail:353951097@qq.com

Analysis and Pre-control Measures for Tripping Caused by Sealing Leakage of Box Substation's Roof

YE Fang-zhou1,GUO Shu-jun2,CUI Shu-juan1   

  1. 1.Cangxian Branch,State Grid Hebei Power Limited Company,061000,Cangzhou,Hebei,China;
    2.Hebei University of Water Resources and Electric Engineering,061001,Cangzhou,Hebei,China

  • Received:2018-06-04 Revised:2018-10-12 Online:2018-12-31 Published:2019-01-31

摘要: 箱式变电站由于长期运行屋顶密封不严,开关柜内出现凝露现象并引发跳闸,文中从故障现象发生到如何处理进行了清晰细致的说明,并提出了合理的预防措施及建议。

关键词: 箱式变, 凝露, 预控措施

Abstract: Since the box substation’s roof is sealed untightly after long-term operation,the condensation arises and then causes tripping in the switchgear.The paper explains the breakdown and the management clearly,and puts forward the reasonable preventive measures and suggestions.

Key words: box substation, condensation, pre-control measures

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